I am an hvac tech and am going on 3 years experience. I have this Lennox rtu Model- LGA120ss1Y Serial- 5600D04459.
It has tons of issues, some history: Another technician went to it and replaced the ignitor, flame sensor, and gas valve. Worked for about 2 days and I got called out to it and it was flashing code 56, air proving switch didn't make or high limit tripped. So I took out my U tube manometer and stuck it right to the draft inducer, had 0"w.c. Took the draft inducer off of the unit and retested 0"w.c. Again. Wheel is fine and not rotted, and secured. So I took a torch tip cleaner and poked out the hole of the inducer housing where the pressure switch hose goes to, then I got 1.5" w.c. Hooked back up and fired every time. Then a few days later another tech went out and not sure what he found then another tech went out and put a washer on the ignitor because he said it wasn't close enough to ignite the flame.
So after that I went back out, about 2 weeks from my original call and had the same exact thing happen, 0"w.c. On the draft motor. I pulled the blower out checked the heat exchanger saw no cracks and I tensioned the belt, etc. Poked a torch tip cleaner all the through the port again and made sure it was open again, checked the hose and all of that and it fired up every time after that. I told the customer and he doesn't believe me at all of what's happening even after he had an employee out there watching over my shoulder.
So the customer said he is going to have his employee pull the heatexchanger and wash it out, blow it out, etc. My opinion is the baffles are rotted and causing debris to get in the port and clog it up but he wasn't buying that argument.
Any tips would be appreciated.
It has tons of issues, some history: Another technician went to it and replaced the ignitor, flame sensor, and gas valve. Worked for about 2 days and I got called out to it and it was flashing code 56, air proving switch didn't make or high limit tripped. So I took out my U tube manometer and stuck it right to the draft inducer, had 0"w.c. Took the draft inducer off of the unit and retested 0"w.c. Again. Wheel is fine and not rotted, and secured. So I took a torch tip cleaner and poked out the hole of the inducer housing where the pressure switch hose goes to, then I got 1.5" w.c. Hooked back up and fired every time. Then a few days later another tech went out and not sure what he found then another tech went out and put a washer on the ignitor because he said it wasn't close enough to ignite the flame.
So after that I went back out, about 2 weeks from my original call and had the same exact thing happen, 0"w.c. On the draft motor. I pulled the blower out checked the heat exchanger saw no cracks and I tensioned the belt, etc. Poked a torch tip cleaner all the through the port again and made sure it was open again, checked the hose and all of that and it fired up every time after that. I told the customer and he doesn't believe me at all of what's happening even after he had an employee out there watching over my shoulder.
So the customer said he is going to have his employee pull the heatexchanger and wash it out, blow it out, etc. My opinion is the baffles are rotted and causing debris to get in the port and clog it up but he wasn't buying that argument.
Any tips would be appreciated.